Composite Flywheel
Background
Philip Medlicott was the inventor and designer of the composite high speed
flywheel (EP 0 145 182) that ran inside the BP KESS (kinetic energy storage
system) vehicle regenerative braking system, developed between 1980 and
1986. Although the BP development is over 35 years old, the technology
and experience is still highly relevant. The BP KESS technology was abruptly
discontinued as a consequence of the changing market conditions arising
from the sudden fall in the oil price in the mid 80's which removed much of
the fuel savings incentive provided by a regenerative braking system.
However, the increases in fuel prices since then, the need to reduce the
carbon footprint and exhaust emissions has resulted in renewed interest in
flywheel technology.
Design concept
The flywheel hub design provided an innovative solution to enable the high
radial strain experienced by the flywheel rim to be coupled with the
relatively small strain found at the shaft. The 1.44 MJ (400 Whr), 460 mm
diameter, 16,000 rpm composite flywheel design was extensively modelled
with FE and validated by spin testing. Other work concentrated on
addressing rotor dynamics and the design of the support system to enable
the flywheel to operate above the critical speed. The flywheel rotor was
supported in the horizontal plane between two sets of matched ball
bearings which themselves were located on squeeze film dampers. The
flywheel was run inside an innovative containment system which provided a
means to withstand the high temperatures and radial loads produced
during the containment event.
System description
The flywheel and containment system operated inside an outer case, which
also provided a means to support the external gearbox. A rotating magnetic
seal on the end of the flywheel shaft enabled the rotor to be run under
vacuum to minimise aerodynamic drag. The system incorporated a
microprocessor based monitoring system to detect the possible early onset
of flywheel failure by monitoring vibration, vacuum, bearing temperature
etc. The manufacture of the flywheel system was based on quantity
production methods to enable a reasonable pay back time on the bases of
savings in operating cost. A subsequent analysis of the manufacturing costs
for the prototype showed that this could be achieved.
The above schematic shows how the flywheel system was coupled to an
early version of the Torrotrack continuously variiable transmission system.
Testing
The system was subjected to several thousand hours (50,000 cycles) of
endurance testing on a test rig where it was cycled between 8,000 and
16,000 rpm. In addition tests were carried out with rotors, some deliberately
damaged, at speeds up to 25,800 rpm to try to initiate a catastrophic failure.
In all cases the failure was initiated by a dynamic instability and resulted in a
benign failure mode, i.e. the rim remained essentially intact, which was an in
keeping with the system design philosophy. Finally the system was tested on
a test track to demonstrate its compatibility with a bus (16 tonne)
environment, for example shock loads from uneven road surfaces. These
tests also included cornering tests at the maximum flywheel design speed
to determine the sensitivity of the flywheel vibration characteristics to large
gyroscopic forces.